Popular Post Mr_Bo11ox Posted February 26, 2018 Popular Post Share Posted February 26, 2018 Anyone remember this from a few months back? Super-basic early X2 Pony. It's in remarkable condition (genuine 26k with no welding or body repairs) but is probably the most miserable joyless vehicle I've yet experienced! 155 X 13 tyres as well.Its been sat on my drive for about 8 months so today I started seeing about getting it ready for an MOT. First off went to motor world for a pair of wiper blades. Easy win. Next, tried to drive it up the drive but there was summert up with the clutch - it would not engage when you took your foot off the pedal!!! FFS man. I fathomed out it was the fault of the clutch shaft that transmits your foot motion from the cable to the thrust bearing. It had only flippin seized up!!! I spent ages trying to free it off but couldnt. Eventually I admited defeat. There was nowt for it but to remove the friggin gearbox!!! So I did that this evening. Can you believe it, I took the gearbox out (only took an hour) then spent almost 2 hours farting about with the clutch shaft, oiling it and twatting it with hammers to loosen it up. drilled a couple of extra holes in the gearbox casing to hel the oil get to where it was needed. After what seemed like a freakin age it was acceptably smooth in operation so I cleaned out the bellhousing and put the box back in, almost giving myself a hernia in the process. Anyway the clutch now works perfectly so I have dropped the dismal old crock in at my local MOT shop - more news tomorrow!!! Dave_Q, ProgRocker, wuvvum and 53 others 56 Link to comment Share on other sites More sharing options...
stillOrange Posted February 26, 2018 Share Posted February 26, 2018 Good luck Pony! Link to comment Share on other sites More sharing options...
spartacus Posted February 26, 2018 Share Posted February 26, 2018 Good work Boll. Do you have any pics of that clutch mechanism, it sounds strange and I can't quite picture it in my head.Good luck on the test. Link to comment Share on other sites More sharing options...
tooSavvy Posted February 26, 2018 Share Posted February 26, 2018 I had a Pony 1.5Auto.... Hmm.. Like driving a fairground bumper car >> noise/acc Saloon = ELECTRIC boot release 'boinggg' FTW TS Cavcraft 1 Link to comment Share on other sites More sharing options...
D Spares & Tyres Posted February 26, 2018 Share Posted February 26, 2018 I rolled one of those once I didn't die 10/10 would roll again fiatdaft, andrew e, HarmonicCheeseburger and 3 others 6 Link to comment Share on other sites More sharing options...
Sigmund Fraud Posted February 26, 2018 Share Posted February 26, 2018 Full points for perseverance ! If it was me, I would have rolled it back out of the workshop and added "free off clutch arm" to my task list (or, rather, task book ; a list doesn't have enough space !). tooSavvy and Talbot 2 Link to comment Share on other sites More sharing options...
UltraWomble Posted February 26, 2018 Share Posted February 26, 2018 Miserable, but almost extinct.One day people will wonder where all these bread and butter cars went and will flock round them at car show like flies around fresh poo, shunning the sea of Minis, Sherpa Coupes and Fraud Escrotes that always seem to be on show. Elstro1988, oldcars, purplebargeken and 1 other 4 Link to comment Share on other sites More sharing options...
Mr_Bo11ox Posted February 26, 2018 Author Share Posted February 26, 2018 Oh dear we've just had a fail Link to comment Share on other sites More sharing options...
strangeangel Posted February 26, 2018 Share Posted February 26, 2018 Oh no. Serious?? Link to comment Share on other sites More sharing options...
Mr_Bo11ox Posted February 26, 2018 Author Share Posted February 26, 2018 Not really, the only thing I'm mildly worried about is the emissions, it doesn't run too well and seemingly its running mega rich. Its got some Japanese carburettor with a million pipes and tubes coming off it so I will have to see if I can do owt with it. I noticed yesterday that some donkey has removed any bypassed the inline pez filter, so some jet or vent is probably blocked purplebargeken and Jim Bell 2 Link to comment Share on other sites More sharing options...
barefoot Posted February 26, 2018 Share Posted February 26, 2018 Oil leak from unexplained holes in gearbox casing? RoadworkUK, HillmanImp, D Spares & Tyres and 4 others 7 Link to comment Share on other sites More sharing options...
Sigmund Fraud Posted February 26, 2018 Share Posted February 26, 2018 This may help with your carb adventures. Link to comment Share on other sites More sharing options...
Mr_Bo11ox Posted February 26, 2018 Author Share Posted February 26, 2018 Just ragged this back from the MOT station. Thanks to the carb problems you have to give it a good caning to make progress but its actually better to drive than i was expecting, got that tight-but-revvy feel that low mileage japanese engines have and it feels like it weighs about 6kg. Will hopefully have a proper look at the carb tomorrow but I think its the same as a Proton 1.3 and there are new and used carbs available for those so I'm sure we can sort something. stephen01, RobT, tooSavvy and 6 others 9 Link to comment Share on other sites More sharing options...
Elstro1988 Posted March 5, 2018 Share Posted March 5, 2018 Please keep this on the road. Old Hyundais are rare as anything and like someone else said, far, far more interesting than the usual showfare. I don't recall the last time I saw a Pony of any age! oldcars 1 Link to comment Share on other sites More sharing options...
Mr_Bo11ox Posted March 5, 2018 Author Share Posted March 5, 2018 Oh yeah I'll get it squared up. I've lost a week of my retest period to freezing weather but nowt gees me up like the thought of chucking £40 away so hopefully I'll get on it this week. egg, Jim Bell, Burnside and 4 others 7 Link to comment Share on other sites More sharing options...
mat_the_cat Posted March 5, 2018 Share Posted March 5, 2018 I don't recall the last time I saw a Pony of any age! But Stellars are common as muck! Good luck with the retest Monsieur sac de balle... purplebargeken, Dick Longbridge, GrumpiusMaximus and 6 others 9 Link to comment Share on other sites More sharing options...
stephen01 Posted March 5, 2018 Share Posted March 5, 2018 I love how having to remove the gearbox is just seen as a slight problem. Top work as always oldcars, tooSavvy, pompei and 1 other 4 Link to comment Share on other sites More sharing options...
Talbot Posted March 6, 2018 Share Posted March 6, 2018 But Stellars are common as muck! Not when that is ALL of them! GrumpiusMaximus and Dick Longbridge 2 Link to comment Share on other sites More sharing options...
Mr_Bo11ox Posted March 6, 2018 Author Share Posted March 6, 2018 Had a look at this tonight. I convinced myself the choke was stuck on. The symptoms are: Emissions test spectacularly failedExhaust fumes stink to high heaven, even when the enigne is fully warmed upengine starts on the button from cold but will not rev up cleanly and will not reach max revs when warm, just fluffs and struggles to get past about 3500-4000 rpm. It defo seems mega rich. SO I pulled the air filter off and had a look. Annoyingly the choke isnt stuck at all. I checked for split pipes and seized up linkages and found none. I really couldnt see owt wrong and there doesnt seem to be any mixture adjustments that can be made so I whipped the carb off to inspect it. One thing I noticed is that the second choke (the lower one in the picture) does not seem to open at all. I thought it was seized so when I had the carb off I inspected it. It's vacuum operated with no direct mechanical connection to the first choke. Its not seized, but there does not seem to be enough vacuum to operate it. I used another pipe to connect it directly to a redundant pipe stub on the inlet manifold and it opens then - the engine sounds fearsome when you're stood over it and the second choke opens, it revs up in a nanosecond. I'm at a bit of a loss really. it seems to be a Mikuni-solex carb, not the same as what you get on a Proton annoyingly but I couldnt find any trakemarks or tags on it so I dont even know what model it is for buying a rebuild kit or whatever. I think you can adjust the idle mixture, but there is clearly something wrong beyond that. You can see the juice trickling out of the main jet when its idling, i'm not sure the idle mixture screw is actually doing anything at all. BAsically I don't really know what to do with it. i dont think I'm gonna find a Mikuni-Solex carburettor specialist who will take a look at it for me..... I might take the carb off again and dismantle it on the bench and see if I can find any split diaphragms or whatever. Any ideas among the shite community? Coprolalia, Jim Bell and M'coli 3 Link to comment Share on other sites More sharing options...
Shep Shepherd Posted March 7, 2018 Share Posted March 7, 2018 http://www.carburettorspecialists.com Any use? yellowperil 1 Link to comment Share on other sites More sharing options...
oldcars Posted March 7, 2018 Share Posted March 7, 2018 Not sure if this is any help? https://www.ebay.co.uk/p/The-Hyundai-Pony-Service-Repair-Manual-by-Mark-Coombs-A-K-Legg-Hardback-1997/91045940?iid=381815323218&_trkparms=aid%3D222007%26algo%3DSIC.MBE%26ao%3D2%26asc%3D49925%26meid%3D82fc20022c044070b18c3cf9f83601a8%26pid%3D100011%26rk%3D1%26rkt%3D1%26sd%3D152888905233%26itm%3D381815323218&_trksid=p2047675.c100011.m1850 Link to comment Share on other sites More sharing options...
Rod/b Posted March 7, 2018 Share Posted March 7, 2018 Any good? https://m.ebay.com/itm/1983-89-CARB-KIT-MITSUBISHI-1-5-2-6L-4-CYLINDER-ENGINES-MIKUNI-SOLEX-2-BARREL/261731645997?fits=Make%3AHyundai&hash=item3cf06bfa2d:g:wOYAAOSwdzVXn7Xi Link to comment Share on other sites More sharing options...
Rod/b Posted March 7, 2018 Share Posted March 7, 2018 Any good? https://m.ebay.com/itm/1983-89-CARB-KIT-MITSUBISHI-1-5-2-6L-4-CYLINDER-ENGINES-MIKUNI-SOLEX-2-BARREL/261731645997?fits=Make%3AHyundai&hash=item3cf06bfa2d:g:wOYAAOSwdzVXn7Xi Or this? https://m.ebay.com/itm/Carb-kit-Dodge-1986-1987-1988-1989-1990-1991-1992-4cyl-Mikuni-Solex-2bbl/332554719134?fits=Make%3AHyundai&hash=item4d6dce4f9e:g:XFwAAOSwwZtaYk2V Link to comment Share on other sites More sharing options...
Junkman Posted March 7, 2018 Share Posted March 7, 2018 It's not a second choke. It's a vacuum operated secondary butterfly.In normal operation it runs only on the primary one, which is operated by the throttle cable.Once this is fully open, the secondary is beginning to open as well, but vacuum operatedby the secondary air valve.There is a lockout that prevents the secondary to open under warm up.I hazard a guess that the choke is maladjusted, so that the lockout remains in placeeven when hot. Nyphur, Dick Longbridge and Coprolalia 3 Link to comment Share on other sites More sharing options...
dave21478 Posted March 7, 2018 Share Posted March 7, 2018 All my previous carburettor related tantrums have been resolved by going to the scrapyard and buying another one. Good luck with that. loserone 1 Link to comment Share on other sites More sharing options...
DodgyBastard Posted March 7, 2018 Share Posted March 7, 2018 https://www.gumtree.com/p/hyundai/hyundai-pony-auto-retro-daily-cheap-runner/1289780053 Just buy this one instead! Link to comment Share on other sites More sharing options...
M'coli Posted March 7, 2018 Share Posted March 7, 2018 I think you can adjust the idle mixture, but there is clearly something wrong beyond that. You can see the juice trickling out of the main jet when its idling, i'm not sure the idle mixture screw is actually doing anything at all. BAsically I don't really know what to do with it. i dont think I'm gonna find a Mikuni-Solex carburettor specialist who will take a look at it for me..... I might take the carb off again and dismantle it on the bench and see if I can find any split diaphragms or whatever. Any ideas among the shite community?Have you had the top off of it to check the usual suspects like the needle valve and the float level? The fuel coming out of the main sort-of flags this up. If you want to try to squeeze it through its retest, it could probably be "jetted down" by sticking strands of fine copper wire down the main jet until it's happy; I've done this in the past for more MPGs although this sounds like it needs something closer to a bit of 0.6 MIG wire in there! Christine 1 Link to comment Share on other sites More sharing options...
Mr_Bo11ox Posted March 8, 2018 Author Share Posted March 8, 2018 No I haven't, but I have been thinking about it all day and I reckon I'm going to remove the carb and do that, check the float level etc as best I can. Also I want to have another look at the mechanism that opens the second butterfly. Even if the whole carb is a mystery, that actuator and mech ought to be simple enough to fathom out. nigel bickle and oldcars 2 Link to comment Share on other sites More sharing options...
mk2_craig Posted March 8, 2018 Share Posted March 8, 2018 Suppose these are too obscure for the likes of Webcon to have ever produced a replacement/upgrade kit? Link to comment Share on other sites More sharing options...
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