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fatharris

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  1. Like
    fatharris got a reaction from Rust Collector in FatHarris - tales of a motoring moron ***Non-BX related content 17/4***   
    Oh christ, I've seen myself off again, haven't I?

    Typically, it's been a very busy fortnight and I've not updated this thread in ages.
    I'll try and break it down into 3-day chunks, because I'm pretty sure the site would have a shitfit if I uploaded 96 photos in one post :lol:

  2. Like
    fatharris got a reaction from Rust Collector in FatHarris - tales of a motoring moron ***Non-BX related content 17/4***   
    No point pussyfooting around it, I had to do one of the most unpleasant jobs on a BX today.
    The steering rack boot - usually a fairly simple swap. Not so with a BX.
    The power steering hydraulic ram is external to the steering rack, so ram eye-end attaches to the nearside rack arm via a protruding lug (shown after I installed the boot)

    First things first, the old one was whipped off. The track rod end was left connected to the hub on each side, and simply unscrewed from the steering rack, to roughly retain the tracking settings.

    The old rack boot had been fouling a bent handbrake cable bracket, and had also dislodged it at one end.

     
    The new boot was thrown into a boiling kettle for a while, in an attempt to soften the boot and give a bit more elasticity. The kitchen drawers were raided for spare spoons, in an attempt to allow the boot to safely stretch over the lug without tearing it. 
    This was a total arseache, compounded by the fact the BX is on the lowest point of the axle stands at the moment. Crawling underneath it every few minutes was a pain, especially with the pigtail hydraulic pipes running through the middle of the engine bay.
    Through divine intervention, I eventually got it on after much swearing. The aftermarket boot was much bigger at one end than the 44mm either side, so a jubilee clip was utilised to evenly take the slack up.

    The other side was a breeze by comparison, and within half an hour, the offside boot was replaced and the track rod ends reconnected. The nearside boot does touch the hydraulic ram, but it shouldn't cause any issues.
    Pretty sure this concludes the jobs around the engine bay. I'm planning to take two days off work next week so I can try and put some graft in to get back on schedule for the target date.
    Oh yeah, here are a few random spots I forgot to post from last week:



    The Xantia was very bouncy on the road, suggesting the spheres are not having a good time.
    Cheers!

  3. Like
    fatharris got a reaction from mat_the_cat in FatHarris - tales of a motoring moron ***Non-BX related content 17/4***   
    Last day of leave from work and once again, no parts arrived. So, more cleaning and little jobs instead.
    The remainder of the gearbox was sprayed with degreaser and left to work in for a bit.
    First shitty job was the bonnet catch.

    Absolutely caked in old sticky grease and grime from 30 years of spraying any old shite onto it.
    Bit more degreaser and some aggressive scrubbing got it looking presentable again.

    Whilst re-lubricating the latch and operating the mechanism, it was clear that something wasn't quite right. The big spring on the left hand dislodged and was gouging into the catch.


    I held the spring in place with steel wire and twatted the top of the bracket to bend it over to retain the screw - job done.

    Was going to adjust the cable as there was quite a lot of slack in the system.

    Nice and simple, just one tiny screw to undo aaaaand...

    Never mind, it works just fine, I was just being picky.
    Next small job, the temperature sensor earth return terminal had came away from the cable - my old crimping tool was well past it. Annoyingly, I ran out of my tiny ring terminals, and with the clearance available, a generic one wouldn't work.

    In the end, I drilled out a male spade terminal to match the screw thread size and it fits perfectly.

    Anyway, with that done, I cracked on, and cleaned the rest of the gearbox up.

    Not perfect, but a hell of a lot better than what it was! Decided there was no better time to change the driveshaft seals. Old ones looked fine, but I had new ones so it made sense to change them!



    Both sides were changed, and rubber grease syringed into the seal cavity.

    I also greased up the gear change rod ball joints.
    In all honesty, there's very little I can do now until the last of the engine parts get here, so I'm going to take a break.
    LOL, as if.

    Herman has been sat on the drive since November, and his MOT has lapsed. There's currently an ABS fault that I need to look into, but as it was the first dry day with no BX work in months, I decided to start small and fit some bits that I've had on the shelf.

    For years and years, I've been told I need to change my throttle cable by Phill because it was corroded and the pedal felt stiff throughout the range of travel. I bought two replacement OE cables last year.
    First up, the throttle pedal cable.

    Surprisingly easy to strip and disconnect at the pedal box end, although the bulkhead clip was a bit of a twat to undo, due to the sound deadening. Brute force force got it out though. Followed the routing and it was adjusted and ready to go, resulting in a much smoother and lighter pedal.

    Next one was even easier, this was for the traction control.
    The actuator had to be unshipped for access to the other side of the cable. With a strong clip either side, I ended up taking it into the garage, clamping the free end of the cable in a vice, applying constant tension to the cable whilst simultaneously undoing both retaining clips.


    But it worked just fine the was a pleasant job.
    Sadly, whilst it needed changing, it wasn't the one I was intending to change, I was after the one for the cruise control actuator:

    The cable in this one is also pretty shagged, and at £90 for a replacement one, I'll be trying my luck at the scrappies in due course. It does work for now so it's not urgent.
    Whilst the airbox was out, I noticed some paint fretting and light corrosion on a contact surface. Treated it with Kurist, and applied some anti-chafing tape to the affected area.
    Anyway, with that all done, it was a quick and easy reassembly.


    Didn't start it up as the battery is still on conditioning charge in the garage.
    Up close, you can see the replacements were required!

    Anyway, I did decide to knock it on the head early for the night. I tidied the tools away and hoovered the garage floor, ready for the next evolution.
    Tomorrow, I'm back to work and we have a torque wrench tester. Going to take mine in so I can see what I need to set the torque wrenches to, in order to get the 20 and 60nm figures required for the head bolt torquing.

    Cheers!
     
     
  4. Like
    fatharris got a reaction from JMotor in FatHarris - tales of a motoring moron ***Non-BX related content 17/4***   
    Last day of leave from work and once again, no parts arrived. So, more cleaning and little jobs instead.
    The remainder of the gearbox was sprayed with degreaser and left to work in for a bit.
    First shitty job was the bonnet catch.

    Absolutely caked in old sticky grease and grime from 30 years of spraying any old shite onto it.
    Bit more degreaser and some aggressive scrubbing got it looking presentable again.

    Whilst re-lubricating the latch and operating the mechanism, it was clear that something wasn't quite right. The big spring on the left hand dislodged and was gouging into the catch.


    I held the spring in place with steel wire and twatted the top of the bracket to bend it over to retain the screw - job done.

    Was going to adjust the cable as there was quite a lot of slack in the system.

    Nice and simple, just one tiny screw to undo aaaaand...

    Never mind, it works just fine, I was just being picky.
    Next small job, the temperature sensor earth return terminal had came away from the cable - my old crimping tool was well past it. Annoyingly, I ran out of my tiny ring terminals, and with the clearance available, a generic one wouldn't work.

    In the end, I drilled out a male spade terminal to match the screw thread size and it fits perfectly.

    Anyway, with that done, I cracked on, and cleaned the rest of the gearbox up.

    Not perfect, but a hell of a lot better than what it was! Decided there was no better time to change the driveshaft seals. Old ones looked fine, but I had new ones so it made sense to change them!



    Both sides were changed, and rubber grease syringed into the seal cavity.

    I also greased up the gear change rod ball joints.
    In all honesty, there's very little I can do now until the last of the engine parts get here, so I'm going to take a break.
    LOL, as if.

    Herman has been sat on the drive since November, and his MOT has lapsed. There's currently an ABS fault that I need to look into, but as it was the first dry day with no BX work in months, I decided to start small and fit some bits that I've had on the shelf.

    For years and years, I've been told I need to change my throttle cable by Phill because it was corroded and the pedal felt stiff throughout the range of travel. I bought two replacement OE cables last year.
    First up, the throttle pedal cable.

    Surprisingly easy to strip and disconnect at the pedal box end, although the bulkhead clip was a bit of a twat to undo, due to the sound deadening. Brute force force got it out though. Followed the routing and it was adjusted and ready to go, resulting in a much smoother and lighter pedal.

    Next one was even easier, this was for the traction control.
    The actuator had to be unshipped for access to the other side of the cable. With a strong clip either side, I ended up taking it into the garage, clamping the free end of the cable in a vice, applying constant tension to the cable whilst simultaneously undoing both retaining clips.


    But it worked just fine the was a pleasant job.
    Sadly, whilst it needed changing, it wasn't the one I was intending to change, I was after the one for the cruise control actuator:

    The cable in this one is also pretty shagged, and at £90 for a replacement one, I'll be trying my luck at the scrappies in due course. It does work for now so it's not urgent.
    Whilst the airbox was out, I noticed some paint fretting and light corrosion on a contact surface. Treated it with Kurist, and applied some anti-chafing tape to the affected area.
    Anyway, with that all done, it was a quick and easy reassembly.


    Didn't start it up as the battery is still on conditioning charge in the garage.
    Up close, you can see the replacements were required!

    Anyway, I did decide to knock it on the head early for the night. I tidied the tools away and hoovered the garage floor, ready for the next evolution.
    Tomorrow, I'm back to work and we have a torque wrench tester. Going to take mine in so I can see what I need to set the torque wrenches to, in order to get the 20 and 60nm figures required for the head bolt torquing.

    Cheers!
     
     
  5. Like
    fatharris reacted to AnnoyingPentium in New wheels - Fantasy Green Skoda Fabia 1.4 OHV   
    This fine motor is the reason I joined here in the first place.
  6. Like
    fatharris got a reaction from Rust Collector in FatHarris - tales of a motoring moron ***Non-BX related content 17/4***   
    Last day of leave from work and once again, no parts arrived. So, more cleaning and little jobs instead.
    The remainder of the gearbox was sprayed with degreaser and left to work in for a bit.
    First shitty job was the bonnet catch.

    Absolutely caked in old sticky grease and grime from 30 years of spraying any old shite onto it.
    Bit more degreaser and some aggressive scrubbing got it looking presentable again.

    Whilst re-lubricating the latch and operating the mechanism, it was clear that something wasn't quite right. The big spring on the left hand dislodged and was gouging into the catch.


    I held the spring in place with steel wire and twatted the top of the bracket to bend it over to retain the screw - job done.

    Was going to adjust the cable as there was quite a lot of slack in the system.

    Nice and simple, just one tiny screw to undo aaaaand...

    Never mind, it works just fine, I was just being picky.
    Next small job, the temperature sensor earth return terminal had came away from the cable - my old crimping tool was well past it. Annoyingly, I ran out of my tiny ring terminals, and with the clearance available, a generic one wouldn't work.

    In the end, I drilled out a male spade terminal to match the screw thread size and it fits perfectly.

    Anyway, with that done, I cracked on, and cleaned the rest of the gearbox up.

    Not perfect, but a hell of a lot better than what it was! Decided there was no better time to change the driveshaft seals. Old ones looked fine, but I had new ones so it made sense to change them!



    Both sides were changed, and rubber grease syringed into the seal cavity.

    I also greased up the gear change rod ball joints.
    In all honesty, there's very little I can do now until the last of the engine parts get here, so I'm going to take a break.
    LOL, as if.

    Herman has been sat on the drive since November, and his MOT has lapsed. There's currently an ABS fault that I need to look into, but as it was the first dry day with no BX work in months, I decided to start small and fit some bits that I've had on the shelf.

    For years and years, I've been told I need to change my throttle cable by Phill because it was corroded and the pedal felt stiff throughout the range of travel. I bought two replacement OE cables last year.
    First up, the throttle pedal cable.

    Surprisingly easy to strip and disconnect at the pedal box end, although the bulkhead clip was a bit of a twat to undo, due to the sound deadening. Brute force force got it out though. Followed the routing and it was adjusted and ready to go, resulting in a much smoother and lighter pedal.

    Next one was even easier, this was for the traction control.
    The actuator had to be unshipped for access to the other side of the cable. With a strong clip either side, I ended up taking it into the garage, clamping the free end of the cable in a vice, applying constant tension to the cable whilst simultaneously undoing both retaining clips.


    But it worked just fine the was a pleasant job.
    Sadly, whilst it needed changing, it wasn't the one I was intending to change, I was after the one for the cruise control actuator:

    The cable in this one is also pretty shagged, and at £90 for a replacement one, I'll be trying my luck at the scrappies in due course. It does work for now so it's not urgent.
    Whilst the airbox was out, I noticed some paint fretting and light corrosion on a contact surface. Treated it with Kurist, and applied some anti-chafing tape to the affected area.
    Anyway, with that all done, it was a quick and easy reassembly.


    Didn't start it up as the battery is still on conditioning charge in the garage.
    Up close, you can see the replacements were required!

    Anyway, I did decide to knock it on the head early for the night. I tidied the tools away and hoovered the garage floor, ready for the next evolution.
    Tomorrow, I'm back to work and we have a torque wrench tester. Going to take mine in so I can see what I need to set the torque wrenches to, in order to get the 20 and 60nm figures required for the head bolt torquing.

    Cheers!
     
     
  7. Like
    fatharris got a reaction from Rust Collector in FatHarris - tales of a motoring moron ***Non-BX related content 17/4***   
    Woke up this morning to find the Rover covered in Saharan dust.



    Quick blast with the hose and it's got the worst of it off.

    Car is loaded and we're ready to go!

    Long old day ahead of us. Setting off now.
  8. Like
    fatharris got a reaction from JMotor in FatHarris - tales of a motoring moron ***Non-BX related content 17/4***   
    Another day with no parts, so it was lots of small jobs to prep for reassembly.
    First job was to source a new set of exhaust manifold studs. As I had a day off work, I went around all the local factors, including an exhaust specialist to get what I needed.
    And I came back empty-handed. Luckily, I've found a company that does the specific studs and nuts for a BX for £11 delivered online, so that'll arrive at some point.
    I also popped into @twosmoke300 who had a camshaft sprocket bolt, as well as lending me a set of engine head stands to check the valve clearances again. These turned out to be okay, only one was just out of limits and it wasn't enough to merit stripping down the head.

    I also removed the fuel manifold pipelines to measure up the required lengths and diameters of pipelines to replace them. Whilst dismantled, I gave the unit a clean, and marked where the pipelines go.

    I did get lucky at the exhaust place though, and got a manifold to downpipe fitting kit - I had to angle grind one of the bolts off during the engine removal.

    The cup washers required a sustained twatting effort to remove, but they gave up the goods eventually and I fitted the new cup washers and the conical mesh gasket. One of the bolts had to be fitted with the washer as it cannot be fitted afterwards.

    I gave the manifold mating faces a bit of a clean and scrub up too.

    Next, I cracked on with the inlet manifold.

    The carb had been replaced during my ownership by Dan, but I had a new set of carb gaskets and it seemed silly to let them go to waste.
    Noticed a little bit of erosion damage on one of the chamfered edges, so I filed it down slightly.

    Removed the old traces of gasket until the face was smooth.

    Then I blanked the holes and got busy with some parts cleaner and a brush - the entirety of the engine bay is bloody filthy, and lagged in a thick coating of oil-based grime.

    After a bit of time, I reassembled the inlet manifold. Looks much cleaner and nicer to handle!

    I also fitted the inlet manifold studs back into the head, after wire brushing the threads, they went back
    Finally, I decided to step away from engine and turn my attention to the next big component awaiting fitment. If the engine was considered dirty, this would be considered filthy.

    Annoyingly, as I removed the clutch arm for access and a re-grease, the pivot bush disintegrated. Annoying, but better it happened now instead of when I put it all back together. £7 for a replacement bush on eBay and we'll cross fingers that it arrives soon.

    The inner bellhousing did clean up nicely though.

    The outside of the box is also taking a bit of time, but there is progress being made.

    You can see the layer of grime I'm having to scrub off here, hopefully I'll finish this job tomorrow morning.

    I'm still waiting for the piston rings and hockey stick seals for No.1 crank bearing to arrive, once they're here I can really get cracking with the rebuild, but I'm not holding out much hope for the NL trip now.
    Not the end of the world as it's been a great target to strive for, but finding faults etc along the way adds extra time to the final date.
    Cheers 😁
  9. Like
    fatharris got a reaction from Rust Collector in FatHarris - tales of a motoring moron ***Non-BX related content 17/4***   
    Another day with no parts, so it was lots of small jobs to prep for reassembly.
    First job was to source a new set of exhaust manifold studs. As I had a day off work, I went around all the local factors, including an exhaust specialist to get what I needed.
    And I came back empty-handed. Luckily, I've found a company that does the specific studs and nuts for a BX for £11 delivered online, so that'll arrive at some point.
    I also popped into @twosmoke300 who had a camshaft sprocket bolt, as well as lending me a set of engine head stands to check the valve clearances again. These turned out to be okay, only one was just out of limits and it wasn't enough to merit stripping down the head.

    I also removed the fuel manifold pipelines to measure up the required lengths and diameters of pipelines to replace them. Whilst dismantled, I gave the unit a clean, and marked where the pipelines go.

    I did get lucky at the exhaust place though, and got a manifold to downpipe fitting kit - I had to angle grind one of the bolts off during the engine removal.

    The cup washers required a sustained twatting effort to remove, but they gave up the goods eventually and I fitted the new cup washers and the conical mesh gasket. One of the bolts had to be fitted with the washer as it cannot be fitted afterwards.

    I gave the manifold mating faces a bit of a clean and scrub up too.

    Next, I cracked on with the inlet manifold.

    The carb had been replaced during my ownership by Dan, but I had a new set of carb gaskets and it seemed silly to let them go to waste.
    Noticed a little bit of erosion damage on one of the chamfered edges, so I filed it down slightly.

    Removed the old traces of gasket until the face was smooth.

    Then I blanked the holes and got busy with some parts cleaner and a brush - the entirety of the engine bay is bloody filthy, and lagged in a thick coating of oil-based grime.

    After a bit of time, I reassembled the inlet manifold. Looks much cleaner and nicer to handle!

    I also fitted the inlet manifold studs back into the head, after wire brushing the threads, they went back
    Finally, I decided to step away from engine and turn my attention to the next big component awaiting fitment. If the engine was considered dirty, this would be considered filthy.

    Annoyingly, as I removed the clutch arm for access and a re-grease, the pivot bush disintegrated. Annoying, but better it happened now instead of when I put it all back together. £7 for a replacement bush on eBay and we'll cross fingers that it arrives soon.

    The inner bellhousing did clean up nicely though.

    The outside of the box is also taking a bit of time, but there is progress being made.

    You can see the layer of grime I'm having to scrub off here, hopefully I'll finish this job tomorrow morning.

    I'm still waiting for the piston rings and hockey stick seals for No.1 crank bearing to arrive, once they're here I can really get cracking with the rebuild, but I'm not holding out much hope for the NL trip now.
    Not the end of the world as it's been a great target to strive for, but finding faults etc along the way adds extra time to the final date.
    Cheers 😁
  10. Like
    fatharris got a reaction from Rust Collector in FatHarris - tales of a motoring moron ***Non-BX related content 17/4***   
    Well, the ferry was an emotional experience - key lowpoint was out overtired 2 year old just wouldn't go to sleep, and kept getting up, and wanting to wander about. I totally understand that, she'd been sat in the car seat for nearly 11 hours at that point.
    They all eventually fell asleep, leaving me to stay too wired to follow them.

    We got out of Dieppe ferry port around 0515, and immediately happened along the Alpine factory 😁

    Didn't realise just how poor the lights got after the beam deflectors were fitted, they were like bloody candles!

    Thankfully, a reinvigorated MrsH had planned ahead and filled a thermos of tea, which was still piping hot the following morning!

    Can tell the British influence in the Rover, it was practically made for this purpose!

    This only worked on the French roads, which were impeccable, with only two potholes observed. Belgian roads are a different kettle of shitey fish altogether.
    Entered NL, and took a quick photo whilst adding to the PC.

    And triumphantly arrived 45 minutes later at my destination, staying with my brother @chatsharris and his wife who has recently had a baby.
    The Rover was absolutely faultless, it worked an absolute treat the entire time and I definitely made the right call to take it. Even the seats that were a bit firm at the beginning, became supportive in the end.
    PC: 7, with one false start.
  11. Like
    fatharris got a reaction from Tickman in FatHarris - tales of a motoring moron ***Non-BX related content 17/4***   
    Another day with no parts, so it was lots of small jobs to prep for reassembly.
    First job was to source a new set of exhaust manifold studs. As I had a day off work, I went around all the local factors, including an exhaust specialist to get what I needed.
    And I came back empty-handed. Luckily, I've found a company that does the specific studs and nuts for a BX for £11 delivered online, so that'll arrive at some point.
    I also popped into @twosmoke300 who had a camshaft sprocket bolt, as well as lending me a set of engine head stands to check the valve clearances again. These turned out to be okay, only one was just out of limits and it wasn't enough to merit stripping down the head.

    I also removed the fuel manifold pipelines to measure up the required lengths and diameters of pipelines to replace them. Whilst dismantled, I gave the unit a clean, and marked where the pipelines go.

    I did get lucky at the exhaust place though, and got a manifold to downpipe fitting kit - I had to angle grind one of the bolts off during the engine removal.

    The cup washers required a sustained twatting effort to remove, but they gave up the goods eventually and I fitted the new cup washers and the conical mesh gasket. One of the bolts had to be fitted with the washer as it cannot be fitted afterwards.

    I gave the manifold mating faces a bit of a clean and scrub up too.

    Next, I cracked on with the inlet manifold.

    The carb had been replaced during my ownership by Dan, but I had a new set of carb gaskets and it seemed silly to let them go to waste.
    Noticed a little bit of erosion damage on one of the chamfered edges, so I filed it down slightly.

    Removed the old traces of gasket until the face was smooth.

    Then I blanked the holes and got busy with some parts cleaner and a brush - the entirety of the engine bay is bloody filthy, and lagged in a thick coating of oil-based grime.

    After a bit of time, I reassembled the inlet manifold. Looks much cleaner and nicer to handle!

    I also fitted the inlet manifold studs back into the head, after wire brushing the threads, they went back
    Finally, I decided to step away from engine and turn my attention to the next big component awaiting fitment. If the engine was considered dirty, this would be considered filthy.

    Annoyingly, as I removed the clutch arm for access and a re-grease, the pivot bush disintegrated. Annoying, but better it happened now instead of when I put it all back together. £7 for a replacement bush on eBay and we'll cross fingers that it arrives soon.

    The inner bellhousing did clean up nicely though.

    The outside of the box is also taking a bit of time, but there is progress being made.

    You can see the layer of grime I'm having to scrub off here, hopefully I'll finish this job tomorrow morning.

    I'm still waiting for the piston rings and hockey stick seals for No.1 crank bearing to arrive, once they're here I can really get cracking with the rebuild, but I'm not holding out much hope for the NL trip now.
    Not the end of the world as it's been a great target to strive for, but finding faults etc along the way adds extra time to the final date.
    Cheers 😁
  12. Like
    fatharris got a reaction from Rust Collector in FatHarris - tales of a motoring moron ***Non-BX related content 17/4***   
    Thank you so much, I really feel it's important to tell it as it happens, warts and all. It certainly almost never goes according to plan but I'm not one to hide the fuckups and failures as it makes for a pretty dull thread otherwise.
    Thankfully @twosmoke300has been absolutely phenomenal with his advice and obscure knowledge, otherwise I'd still be curled up in a corner of the room sobbing 😅
     
  13. Like
    fatharris got a reaction from JakeT in FatHarris - tales of a motoring moron ***Non-BX related content 17/4***   
    Another day with no parts, so it was lots of small jobs to prep for reassembly.
    First job was to source a new set of exhaust manifold studs. As I had a day off work, I went around all the local factors, including an exhaust specialist to get what I needed.
    And I came back empty-handed. Luckily, I've found a company that does the specific studs and nuts for a BX for £11 delivered online, so that'll arrive at some point.
    I also popped into @twosmoke300 who had a camshaft sprocket bolt, as well as lending me a set of engine head stands to check the valve clearances again. These turned out to be okay, only one was just out of limits and it wasn't enough to merit stripping down the head.

    I also removed the fuel manifold pipelines to measure up the required lengths and diameters of pipelines to replace them. Whilst dismantled, I gave the unit a clean, and marked where the pipelines go.

    I did get lucky at the exhaust place though, and got a manifold to downpipe fitting kit - I had to angle grind one of the bolts off during the engine removal.

    The cup washers required a sustained twatting effort to remove, but they gave up the goods eventually and I fitted the new cup washers and the conical mesh gasket. One of the bolts had to be fitted with the washer as it cannot be fitted afterwards.

    I gave the manifold mating faces a bit of a clean and scrub up too.

    Next, I cracked on with the inlet manifold.

    The carb had been replaced during my ownership by Dan, but I had a new set of carb gaskets and it seemed silly to let them go to waste.
    Noticed a little bit of erosion damage on one of the chamfered edges, so I filed it down slightly.

    Removed the old traces of gasket until the face was smooth.

    Then I blanked the holes and got busy with some parts cleaner and a brush - the entirety of the engine bay is bloody filthy, and lagged in a thick coating of oil-based grime.

    After a bit of time, I reassembled the inlet manifold. Looks much cleaner and nicer to handle!

    I also fitted the inlet manifold studs back into the head, after wire brushing the threads, they went back
    Finally, I decided to step away from engine and turn my attention to the next big component awaiting fitment. If the engine was considered dirty, this would be considered filthy.

    Annoyingly, as I removed the clutch arm for access and a re-grease, the pivot bush disintegrated. Annoying, but better it happened now instead of when I put it all back together. £7 for a replacement bush on eBay and we'll cross fingers that it arrives soon.

    The inner bellhousing did clean up nicely though.

    The outside of the box is also taking a bit of time, but there is progress being made.

    You can see the layer of grime I'm having to scrub off here, hopefully I'll finish this job tomorrow morning.

    I'm still waiting for the piston rings and hockey stick seals for No.1 crank bearing to arrive, once they're here I can really get cracking with the rebuild, but I'm not holding out much hope for the NL trip now.
    Not the end of the world as it's been a great target to strive for, but finding faults etc along the way adds extra time to the final date.
    Cheers 😁
  14. Like
    fatharris got a reaction from Jenson Velcro in FatHarris - tales of a motoring moron ***Non-BX related content 17/4***   
    Another day with no parts, so it was lots of small jobs to prep for reassembly.
    First job was to source a new set of exhaust manifold studs. As I had a day off work, I went around all the local factors, including an exhaust specialist to get what I needed.
    And I came back empty-handed. Luckily, I've found a company that does the specific studs and nuts for a BX for £11 delivered online, so that'll arrive at some point.
    I also popped into @twosmoke300 who had a camshaft sprocket bolt, as well as lending me a set of engine head stands to check the valve clearances again. These turned out to be okay, only one was just out of limits and it wasn't enough to merit stripping down the head.

    I also removed the fuel manifold pipelines to measure up the required lengths and diameters of pipelines to replace them. Whilst dismantled, I gave the unit a clean, and marked where the pipelines go.

    I did get lucky at the exhaust place though, and got a manifold to downpipe fitting kit - I had to angle grind one of the bolts off during the engine removal.

    The cup washers required a sustained twatting effort to remove, but they gave up the goods eventually and I fitted the new cup washers and the conical mesh gasket. One of the bolts had to be fitted with the washer as it cannot be fitted afterwards.

    I gave the manifold mating faces a bit of a clean and scrub up too.

    Next, I cracked on with the inlet manifold.

    The carb had been replaced during my ownership by Dan, but I had a new set of carb gaskets and it seemed silly to let them go to waste.
    Noticed a little bit of erosion damage on one of the chamfered edges, so I filed it down slightly.

    Removed the old traces of gasket until the face was smooth.

    Then I blanked the holes and got busy with some parts cleaner and a brush - the entirety of the engine bay is bloody filthy, and lagged in a thick coating of oil-based grime.

    After a bit of time, I reassembled the inlet manifold. Looks much cleaner and nicer to handle!

    I also fitted the inlet manifold studs back into the head, after wire brushing the threads, they went back
    Finally, I decided to step away from engine and turn my attention to the next big component awaiting fitment. If the engine was considered dirty, this would be considered filthy.

    Annoyingly, as I removed the clutch arm for access and a re-grease, the pivot bush disintegrated. Annoying, but better it happened now instead of when I put it all back together. £7 for a replacement bush on eBay and we'll cross fingers that it arrives soon.

    The inner bellhousing did clean up nicely though.

    The outside of the box is also taking a bit of time, but there is progress being made.

    You can see the layer of grime I'm having to scrub off here, hopefully I'll finish this job tomorrow morning.

    I'm still waiting for the piston rings and hockey stick seals for No.1 crank bearing to arrive, once they're here I can really get cracking with the rebuild, but I'm not holding out much hope for the NL trip now.
    Not the end of the world as it's been a great target to strive for, but finding faults etc along the way adds extra time to the final date.
    Cheers 😁
  15. Like
    fatharris got a reaction from mercedade in FatHarris - tales of a motoring moron ***Non-BX related content 17/4***   
    Another day with no parts, so it was lots of small jobs to prep for reassembly.
    First job was to source a new set of exhaust manifold studs. As I had a day off work, I went around all the local factors, including an exhaust specialist to get what I needed.
    And I came back empty-handed. Luckily, I've found a company that does the specific studs and nuts for a BX for £11 delivered online, so that'll arrive at some point.
    I also popped into @twosmoke300 who had a camshaft sprocket bolt, as well as lending me a set of engine head stands to check the valve clearances again. These turned out to be okay, only one was just out of limits and it wasn't enough to merit stripping down the head.

    I also removed the fuel manifold pipelines to measure up the required lengths and diameters of pipelines to replace them. Whilst dismantled, I gave the unit a clean, and marked where the pipelines go.

    I did get lucky at the exhaust place though, and got a manifold to downpipe fitting kit - I had to angle grind one of the bolts off during the engine removal.

    The cup washers required a sustained twatting effort to remove, but they gave up the goods eventually and I fitted the new cup washers and the conical mesh gasket. One of the bolts had to be fitted with the washer as it cannot be fitted afterwards.

    I gave the manifold mating faces a bit of a clean and scrub up too.

    Next, I cracked on with the inlet manifold.

    The carb had been replaced during my ownership by Dan, but I had a new set of carb gaskets and it seemed silly to let them go to waste.
    Noticed a little bit of erosion damage on one of the chamfered edges, so I filed it down slightly.

    Removed the old traces of gasket until the face was smooth.

    Then I blanked the holes and got busy with some parts cleaner and a brush - the entirety of the engine bay is bloody filthy, and lagged in a thick coating of oil-based grime.

    After a bit of time, I reassembled the inlet manifold. Looks much cleaner and nicer to handle!

    I also fitted the inlet manifold studs back into the head, after wire brushing the threads, they went back
    Finally, I decided to step away from engine and turn my attention to the next big component awaiting fitment. If the engine was considered dirty, this would be considered filthy.

    Annoyingly, as I removed the clutch arm for access and a re-grease, the pivot bush disintegrated. Annoying, but better it happened now instead of when I put it all back together. £7 for a replacement bush on eBay and we'll cross fingers that it arrives soon.

    The inner bellhousing did clean up nicely though.

    The outside of the box is also taking a bit of time, but there is progress being made.

    You can see the layer of grime I'm having to scrub off here, hopefully I'll finish this job tomorrow morning.

    I'm still waiting for the piston rings and hockey stick seals for No.1 crank bearing to arrive, once they're here I can really get cracking with the rebuild, but I'm not holding out much hope for the NL trip now.
    Not the end of the world as it's been a great target to strive for, but finding faults etc along the way adds extra time to the final date.
    Cheers 😁
  16. Like
    fatharris got a reaction from Stanky in FatHarris - tales of a motoring moron ***Non-BX related content 17/4***   
    Another day with no parts, so it was lots of small jobs to prep for reassembly.
    First job was to source a new set of exhaust manifold studs. As I had a day off work, I went around all the local factors, including an exhaust specialist to get what I needed.
    And I came back empty-handed. Luckily, I've found a company that does the specific studs and nuts for a BX for £11 delivered online, so that'll arrive at some point.
    I also popped into @twosmoke300 who had a camshaft sprocket bolt, as well as lending me a set of engine head stands to check the valve clearances again. These turned out to be okay, only one was just out of limits and it wasn't enough to merit stripping down the head.

    I also removed the fuel manifold pipelines to measure up the required lengths and diameters of pipelines to replace them. Whilst dismantled, I gave the unit a clean, and marked where the pipelines go.

    I did get lucky at the exhaust place though, and got a manifold to downpipe fitting kit - I had to angle grind one of the bolts off during the engine removal.

    The cup washers required a sustained twatting effort to remove, but they gave up the goods eventually and I fitted the new cup washers and the conical mesh gasket. One of the bolts had to be fitted with the washer as it cannot be fitted afterwards.

    I gave the manifold mating faces a bit of a clean and scrub up too.

    Next, I cracked on with the inlet manifold.

    The carb had been replaced during my ownership by Dan, but I had a new set of carb gaskets and it seemed silly to let them go to waste.
    Noticed a little bit of erosion damage on one of the chamfered edges, so I filed it down slightly.

    Removed the old traces of gasket until the face was smooth.

    Then I blanked the holes and got busy with some parts cleaner and a brush - the entirety of the engine bay is bloody filthy, and lagged in a thick coating of oil-based grime.

    After a bit of time, I reassembled the inlet manifold. Looks much cleaner and nicer to handle!

    I also fitted the inlet manifold studs back into the head, after wire brushing the threads, they went back
    Finally, I decided to step away from engine and turn my attention to the next big component awaiting fitment. If the engine was considered dirty, this would be considered filthy.

    Annoyingly, as I removed the clutch arm for access and a re-grease, the pivot bush disintegrated. Annoying, but better it happened now instead of when I put it all back together. £7 for a replacement bush on eBay and we'll cross fingers that it arrives soon.

    The inner bellhousing did clean up nicely though.

    The outside of the box is also taking a bit of time, but there is progress being made.

    You can see the layer of grime I'm having to scrub off here, hopefully I'll finish this job tomorrow morning.

    I'm still waiting for the piston rings and hockey stick seals for No.1 crank bearing to arrive, once they're here I can really get cracking with the rebuild, but I'm not holding out much hope for the NL trip now.
    Not the end of the world as it's been a great target to strive for, but finding faults etc along the way adds extra time to the final date.
    Cheers 😁
  17. Like
    fatharris reacted to mk2_craig in FatHarris - tales of a motoring moron ***Non-BX related content 17/4***   
    One of my favourite threads right now. This car has a bright future having had all this care and attention given to it. 
  18. Like
    fatharris got a reaction from Rust Collector in FatHarris - tales of a motoring moron ***Non-BX related content 17/4***   
    Been a lot of hits and misses this weekend.
    First up, trying to torque the camshaft cap studs was a pain, 15nm was simply not happening, even with the two nuts tight against each other, it was still turning down the shaft when close to 15nm. Tried adding a third nut to see if that would help matters, but ended up stripping the threads on the nut.
    In the end, I went for 10nm. It'll be fine, I hope. Fitted the cam, and new front cam seal before I torqued down the caps (minus one nut).

    Then it came to the camshaft pulley. Following the torque figure, I didn't even get close to the Haynes figure before disaster struck.


    That was....not ideal. I messaged Phill on a blind panic asking for advice, and he suggested drilling a 3mm hole in the bolt shank and hammering a torx socket into the hole to extract it. There were almost tears of joy when this came out.

    Then joy turned into anger when I decided to check the figures in my Autodata technical data book.
    Haynes (stated 80nm) for the sprocket bolt.

    Autodata?

    So the bolt failure was caused by a massive overtorque. Arse biscuits.
    To try and take my mind off it, I tackled some of the minor jobs, first job was removing and re-sealing the body seams around the bootlid hinge. Forgot to get any photos, but I scraped the old, dry seam sealer with a plastic scraper, masked the area off with tape and applied a healthy layer or Pureaflex40 to the joins.
    Whilst I was in the area, I managed to push the split section of the wiring rubber grommet into the hole, so it'll be a much better seal than the empty space that was there before!
    I continued the minor jobs, treating screen rust spots before they become sinister,

    Swapping out the rocker cover gasket:

    And getting this dirty bottle cleaned up as much as possible.

    Which cleaned up alright, but had highlighted how big the crack in the side of the tank was:

    As it was the rarely-used rear washer tank, I elected to try and repair it rather than replace. I used an old soldering iron to re-melt the plastic along the crack. It's not pretty, but it's sealed up and shouldn't leak so that's a win.

    The bottoms of these bottles have a sharp lip around their manufacturing joins which has been suggested aids corrosion by chafing through the paint - these were sanded down prior to install. The scuttle area had already been heavily lanoguarded about six weeks ago so all should be well there.
    Unrelated to the BX, but a mate  followed me on the commute to work and told me one of the Rovers brake lights wasn't coming on every time. Luckily, I have spare bulbs, but it was quite interesting to see the where the filament had broken loose, flapped around a bit until it made the circuit and 'tacked' itself back on. Herman has had a front fog light doing that for years, so the build-up there must be spectacular.

    Eventually, I decided to carry on with assembling the 3 pistons and liners, I'm still awaiting parts to assemble the final cylinder but this is a good start.
    Turns out I needed to order another set of piston rings too, thanks to my ill-fated attempt to fit them last time:

    Annoyingly, this was a pain in the arse. Autodoc did them at a reasonable price, but the delivery time takes the piss at around a fortnight. I found some on eBay with a two day delivery, so I placed the order on Sunday. I then sent the seller my details, and they cancelled the order! Apparently they weren't compatible. I've told them I want the rings and will assume the risk - the manufacturers of the piston rings list the set as compatible for every 1.6 XU engine except the XU52C. I can't see what difference there would be though, so I guess we'll find out in a couple of days.
    Anyway, the ring gaps were checked prior to fitment, they were all bang on at around 0.50mm.


    With the new set of plier-style piston ring compressors, I was STILL having issues with the rings. 
    I asked Phill for advice, and he very gently pointed out I was being a bit of a fuckwit and assembling the oil control ring at the bottom incorrectly, which in turn meant the ring wasn't compressing properly. 
    With the correct advice dispensed, and a slight tweak to the piston ring compressor, we were finally making progress! A fresh seal was fitted to the base of the cylinder liner before slotting it into place.

    Eventually, I got all three complete assemblies in.

    And clamped the liners down.

    Then I nipped back to the house for a pee, and noticed that Mini had snuck into MrsH's car whilst she was unloading, and got himself locked in. Tit.

    I decided to crack on with bolting in some external components, so the oil pressure switch, water pump and timing belt tensioner pulley went on (the old one was really rather grumbly and rattly)
    The pump came from Autodoc and was their own brand (RIDEX) and it seemed pretty well made.

    Next up, the crank bearing seats were cleaned, new shells were fitted, and the crank lowered into place. This was a pain in the arse with the liners and pistons fitted as the conrods were in the way, this was aided with some steel wire to hold them in the middle position.

    The crank bearing caps had fresh shells and an oiling before being loosely assembled.

    I'm still awaiting the seals for No.1 bearing cap so I've not fitted that yet.
    After that, it was applying the last coat of lacquer to the windscreen frame rust spots. The paint colour match is pretty poor, but it won't rust and that's what matters.
    I spent the remainder of the evening googling part numbers, dimensions and specs of the cam cap nut. The Citroen parts catalogue specified a nut and washer assembly, the Peugeot catalogue specified a flange nut. Seeing as this was what was fitted, I went with that, got the size and thread pitch and started searching. I eventually got three part numbers, and the phone numbers for potential dealerships that could have the nut I need in stock.
    A bit of phoning around yesterday morning ensued. The Peugeot dealership said they could source the nuts, but they wouldn't be here till Wednesday and were £1.25 each.
    My second dealership took the part number, said 'Yep, we've got 14 in stock here, and they're 63p each+VAT'. Didn't bother ringing the third.
    The dealership?

    Yep, I went in my Rover that's really a Honda, to a BMW dealership to pick up some nuts for my Citroen, which was sourced using specs from a Peugeot parts catalogue.

    The parts fella that came out was very friendly, and couldn't believe what vehicle the nuts were for I ended up having a chat with him about the Rover parked outside and he was really enthusiastic. Ended up buying 10 nuts as it makes sense to replace the entire set.
    Got home and checked the nut - it's a good fit, a bit taller and with a wider flange than the originals, it feels much more substantial. The nut is originally used to hold inlet manifolds onto various BMWs.
    I started checking valve clearances but this ended up being a pain to rotate the camshaft without the sprocket bolted in. I checked the first 4 and found them to be juuuuust within limits, I'll check the other 4 later when I've got the camshaft bolt and torqued it in.
    Boring stuff, but prepping for when it gets reassembled, the fuel pump gaskets were changed, thedistributor oil seal was replaced:

    And the inlet manifold gasket was tackled. 

    This took an absolute eternity - it was properly on there! The mating faces were eventually cleaned with a scotchbrite pad and WD40 to get a smoother mating face.

    Today, I'm into my two days off that was pencilled in for engine building - not much bloody use of I've not got all the parts together! I'll be working on various other little jobs instead.
    Cheers.


  19. Like
    fatharris got a reaction from Rust Collector in FatHarris - tales of a motoring moron ***Non-BX related content 17/4***   
    Well, the block is on hold until I get the new tooling and spares, so may as well crack on with the head. I've moved my leave at work one day later to Tuesday and Wednesday to work on the block - hopefully everything arrives before then 🤠
    Starting with lapping the valves.

    This was actually one of the most relaxing jobs I've done on this car. Nice and steady, and taking my time.
    Results are promising too.




    Should help keep the head a bit more gastight!
    After a lot of tweezer action, fangs, and the air gun, I got the majority of the swarf out of the head chambers, I installed the valve stem seals - piece of cake with the insertion tool that came with the removal pliers.

    Finally, it was time to re-introduce this haggard lash-up to reassemble the valves!

    I was unsure if this was going to work this time around, but thankfully it did!

    With the stems lubed and the collets greased, everything came together nicely and all 8 valves were fitted.

    After that, the tappets and shims were greased/lubed and fitted, and the camshaft studs fitted. Going to check torque them again with the advice from @red5 (Thanks mate!).
    But first, it's breakfast time.

  20. Like
    fatharris got a reaction from GeorgeB in FatHarris - tales of a motoring moron ***Non-BX related content 17/4***   
    Been a lot of hits and misses this weekend.
    First up, trying to torque the camshaft cap studs was a pain, 15nm was simply not happening, even with the two nuts tight against each other, it was still turning down the shaft when close to 15nm. Tried adding a third nut to see if that would help matters, but ended up stripping the threads on the nut.
    In the end, I went for 10nm. It'll be fine, I hope. Fitted the cam, and new front cam seal before I torqued down the caps (minus one nut).

    Then it came to the camshaft pulley. Following the torque figure, I didn't even get close to the Haynes figure before disaster struck.


    That was....not ideal. I messaged Phill on a blind panic asking for advice, and he suggested drilling a 3mm hole in the bolt shank and hammering a torx socket into the hole to extract it. There were almost tears of joy when this came out.

    Then joy turned into anger when I decided to check the figures in my Autodata technical data book.
    Haynes (stated 80nm) for the sprocket bolt.

    Autodata?

    So the bolt failure was caused by a massive overtorque. Arse biscuits.
    To try and take my mind off it, I tackled some of the minor jobs, first job was removing and re-sealing the body seams around the bootlid hinge. Forgot to get any photos, but I scraped the old, dry seam sealer with a plastic scraper, masked the area off with tape and applied a healthy layer or Pureaflex40 to the joins.
    Whilst I was in the area, I managed to push the split section of the wiring rubber grommet into the hole, so it'll be a much better seal than the empty space that was there before!
    I continued the minor jobs, treating screen rust spots before they become sinister,

    Swapping out the rocker cover gasket:

    And getting this dirty bottle cleaned up as much as possible.

    Which cleaned up alright, but had highlighted how big the crack in the side of the tank was:

    As it was the rarely-used rear washer tank, I elected to try and repair it rather than replace. I used an old soldering iron to re-melt the plastic along the crack. It's not pretty, but it's sealed up and shouldn't leak so that's a win.

    The bottoms of these bottles have a sharp lip around their manufacturing joins which has been suggested aids corrosion by chafing through the paint - these were sanded down prior to install. The scuttle area had already been heavily lanoguarded about six weeks ago so all should be well there.
    Unrelated to the BX, but a mate  followed me on the commute to work and told me one of the Rovers brake lights wasn't coming on every time. Luckily, I have spare bulbs, but it was quite interesting to see the where the filament had broken loose, flapped around a bit until it made the circuit and 'tacked' itself back on. Herman has had a front fog light doing that for years, so the build-up there must be spectacular.

    Eventually, I decided to carry on with assembling the 3 pistons and liners, I'm still awaiting parts to assemble the final cylinder but this is a good start.
    Turns out I needed to order another set of piston rings too, thanks to my ill-fated attempt to fit them last time:

    Annoyingly, this was a pain in the arse. Autodoc did them at a reasonable price, but the delivery time takes the piss at around a fortnight. I found some on eBay with a two day delivery, so I placed the order on Sunday. I then sent the seller my details, and they cancelled the order! Apparently they weren't compatible. I've told them I want the rings and will assume the risk - the manufacturers of the piston rings list the set as compatible for every 1.6 XU engine except the XU52C. I can't see what difference there would be though, so I guess we'll find out in a couple of days.
    Anyway, the ring gaps were checked prior to fitment, they were all bang on at around 0.50mm.


    With the new set of plier-style piston ring compressors, I was STILL having issues with the rings. 
    I asked Phill for advice, and he very gently pointed out I was being a bit of a fuckwit and assembling the oil control ring at the bottom incorrectly, which in turn meant the ring wasn't compressing properly. 
    With the correct advice dispensed, and a slight tweak to the piston ring compressor, we were finally making progress! A fresh seal was fitted to the base of the cylinder liner before slotting it into place.

    Eventually, I got all three complete assemblies in.

    And clamped the liners down.

    Then I nipped back to the house for a pee, and noticed that Mini had snuck into MrsH's car whilst she was unloading, and got himself locked in. Tit.

    I decided to crack on with bolting in some external components, so the oil pressure switch, water pump and timing belt tensioner pulley went on (the old one was really rather grumbly and rattly)
    The pump came from Autodoc and was their own brand (RIDEX) and it seemed pretty well made.

    Next up, the crank bearing seats were cleaned, new shells were fitted, and the crank lowered into place. This was a pain in the arse with the liners and pistons fitted as the conrods were in the way, this was aided with some steel wire to hold them in the middle position.

    The crank bearing caps had fresh shells and an oiling before being loosely assembled.

    I'm still awaiting the seals for No.1 bearing cap so I've not fitted that yet.
    After that, it was applying the last coat of lacquer to the windscreen frame rust spots. The paint colour match is pretty poor, but it won't rust and that's what matters.
    I spent the remainder of the evening googling part numbers, dimensions and specs of the cam cap nut. The Citroen parts catalogue specified a nut and washer assembly, the Peugeot catalogue specified a flange nut. Seeing as this was what was fitted, I went with that, got the size and thread pitch and started searching. I eventually got three part numbers, and the phone numbers for potential dealerships that could have the nut I need in stock.
    A bit of phoning around yesterday morning ensued. The Peugeot dealership said they could source the nuts, but they wouldn't be here till Wednesday and were £1.25 each.
    My second dealership took the part number, said 'Yep, we've got 14 in stock here, and they're 63p each+VAT'. Didn't bother ringing the third.
    The dealership?

    Yep, I went in my Rover that's really a Honda, to a BMW dealership to pick up some nuts for my Citroen, which was sourced using specs from a Peugeot parts catalogue.

    The parts fella that came out was very friendly, and couldn't believe what vehicle the nuts were for I ended up having a chat with him about the Rover parked outside and he was really enthusiastic. Ended up buying 10 nuts as it makes sense to replace the entire set.
    Got home and checked the nut - it's a good fit, a bit taller and with a wider flange than the originals, it feels much more substantial. The nut is originally used to hold inlet manifolds onto various BMWs.
    I started checking valve clearances but this ended up being a pain to rotate the camshaft without the sprocket bolted in. I checked the first 4 and found them to be juuuuust within limits, I'll check the other 4 later when I've got the camshaft bolt and torqued it in.
    Boring stuff, but prepping for when it gets reassembled, the fuel pump gaskets were changed, thedistributor oil seal was replaced:

    And the inlet manifold gasket was tackled. 

    This took an absolute eternity - it was properly on there! The mating faces were eventually cleaned with a scotchbrite pad and WD40 to get a smoother mating face.

    Today, I'm into my two days off that was pencilled in for engine building - not much bloody use of I've not got all the parts together! I'll be working on various other little jobs instead.
    Cheers.


  21. Like
    fatharris got a reaction from Dyslexic Viking in FatHarris - tales of a motoring moron ***Non-BX related content 17/4***   
    Been a lot of hits and misses this weekend.
    First up, trying to torque the camshaft cap studs was a pain, 15nm was simply not happening, even with the two nuts tight against each other, it was still turning down the shaft when close to 15nm. Tried adding a third nut to see if that would help matters, but ended up stripping the threads on the nut.
    In the end, I went for 10nm. It'll be fine, I hope. Fitted the cam, and new front cam seal before I torqued down the caps (minus one nut).

    Then it came to the camshaft pulley. Following the torque figure, I didn't even get close to the Haynes figure before disaster struck.


    That was....not ideal. I messaged Phill on a blind panic asking for advice, and he suggested drilling a 3mm hole in the bolt shank and hammering a torx socket into the hole to extract it. There were almost tears of joy when this came out.

    Then joy turned into anger when I decided to check the figures in my Autodata technical data book.
    Haynes (stated 80nm) for the sprocket bolt.

    Autodata?

    So the bolt failure was caused by a massive overtorque. Arse biscuits.
    To try and take my mind off it, I tackled some of the minor jobs, first job was removing and re-sealing the body seams around the bootlid hinge. Forgot to get any photos, but I scraped the old, dry seam sealer with a plastic scraper, masked the area off with tape and applied a healthy layer or Pureaflex40 to the joins.
    Whilst I was in the area, I managed to push the split section of the wiring rubber grommet into the hole, so it'll be a much better seal than the empty space that was there before!
    I continued the minor jobs, treating screen rust spots before they become sinister,

    Swapping out the rocker cover gasket:

    And getting this dirty bottle cleaned up as much as possible.

    Which cleaned up alright, but had highlighted how big the crack in the side of the tank was:

    As it was the rarely-used rear washer tank, I elected to try and repair it rather than replace. I used an old soldering iron to re-melt the plastic along the crack. It's not pretty, but it's sealed up and shouldn't leak so that's a win.

    The bottoms of these bottles have a sharp lip around their manufacturing joins which has been suggested aids corrosion by chafing through the paint - these were sanded down prior to install. The scuttle area had already been heavily lanoguarded about six weeks ago so all should be well there.
    Unrelated to the BX, but a mate  followed me on the commute to work and told me one of the Rovers brake lights wasn't coming on every time. Luckily, I have spare bulbs, but it was quite interesting to see the where the filament had broken loose, flapped around a bit until it made the circuit and 'tacked' itself back on. Herman has had a front fog light doing that for years, so the build-up there must be spectacular.

    Eventually, I decided to carry on with assembling the 3 pistons and liners, I'm still awaiting parts to assemble the final cylinder but this is a good start.
    Turns out I needed to order another set of piston rings too, thanks to my ill-fated attempt to fit them last time:

    Annoyingly, this was a pain in the arse. Autodoc did them at a reasonable price, but the delivery time takes the piss at around a fortnight. I found some on eBay with a two day delivery, so I placed the order on Sunday. I then sent the seller my details, and they cancelled the order! Apparently they weren't compatible. I've told them I want the rings and will assume the risk - the manufacturers of the piston rings list the set as compatible for every 1.6 XU engine except the XU52C. I can't see what difference there would be though, so I guess we'll find out in a couple of days.
    Anyway, the ring gaps were checked prior to fitment, they were all bang on at around 0.50mm.


    With the new set of plier-style piston ring compressors, I was STILL having issues with the rings. 
    I asked Phill for advice, and he very gently pointed out I was being a bit of a fuckwit and assembling the oil control ring at the bottom incorrectly, which in turn meant the ring wasn't compressing properly. 
    With the correct advice dispensed, and a slight tweak to the piston ring compressor, we were finally making progress! A fresh seal was fitted to the base of the cylinder liner before slotting it into place.

    Eventually, I got all three complete assemblies in.

    And clamped the liners down.

    Then I nipped back to the house for a pee, and noticed that Mini had snuck into MrsH's car whilst she was unloading, and got himself locked in. Tit.

    I decided to crack on with bolting in some external components, so the oil pressure switch, water pump and timing belt tensioner pulley went on (the old one was really rather grumbly and rattly)
    The pump came from Autodoc and was their own brand (RIDEX) and it seemed pretty well made.

    Next up, the crank bearing seats were cleaned, new shells were fitted, and the crank lowered into place. This was a pain in the arse with the liners and pistons fitted as the conrods were in the way, this was aided with some steel wire to hold them in the middle position.

    The crank bearing caps had fresh shells and an oiling before being loosely assembled.

    I'm still awaiting the seals for No.1 bearing cap so I've not fitted that yet.
    After that, it was applying the last coat of lacquer to the windscreen frame rust spots. The paint colour match is pretty poor, but it won't rust and that's what matters.
    I spent the remainder of the evening googling part numbers, dimensions and specs of the cam cap nut. The Citroen parts catalogue specified a nut and washer assembly, the Peugeot catalogue specified a flange nut. Seeing as this was what was fitted, I went with that, got the size and thread pitch and started searching. I eventually got three part numbers, and the phone numbers for potential dealerships that could have the nut I need in stock.
    A bit of phoning around yesterday morning ensued. The Peugeot dealership said they could source the nuts, but they wouldn't be here till Wednesday and were £1.25 each.
    My second dealership took the part number, said 'Yep, we've got 14 in stock here, and they're 63p each+VAT'. Didn't bother ringing the third.
    The dealership?

    Yep, I went in my Rover that's really a Honda, to a BMW dealership to pick up some nuts for my Citroen, which was sourced using specs from a Peugeot parts catalogue.

    The parts fella that came out was very friendly, and couldn't believe what vehicle the nuts were for I ended up having a chat with him about the Rover parked outside and he was really enthusiastic. Ended up buying 10 nuts as it makes sense to replace the entire set.
    Got home and checked the nut - it's a good fit, a bit taller and with a wider flange than the originals, it feels much more substantial. The nut is originally used to hold inlet manifolds onto various BMWs.
    I started checking valve clearances but this ended up being a pain to rotate the camshaft without the sprocket bolted in. I checked the first 4 and found them to be juuuuust within limits, I'll check the other 4 later when I've got the camshaft bolt and torqued it in.
    Boring stuff, but prepping for when it gets reassembled, the fuel pump gaskets were changed, thedistributor oil seal was replaced:

    And the inlet manifold gasket was tackled. 

    This took an absolute eternity - it was properly on there! The mating faces were eventually cleaned with a scotchbrite pad and WD40 to get a smoother mating face.

    Today, I'm into my two days off that was pencilled in for engine building - not much bloody use of I've not got all the parts together! I'll be working on various other little jobs instead.
    Cheers.


  22. Like
    fatharris got a reaction from Tickman in FatHarris - tales of a motoring moron ***Non-BX related content 17/4***   
    Thank you so much, I really feel it's important to tell it as it happens, warts and all. It certainly almost never goes according to plan but I'm not one to hide the fuckups and failures as it makes for a pretty dull thread otherwise.
    Thankfully @twosmoke300has been absolutely phenomenal with his advice and obscure knowledge, otherwise I'd still be curled up in a corner of the room sobbing 😅
     
  23. Thanks
    fatharris got a reaction from mercedade in FatHarris - tales of a motoring moron ***Non-BX related content 17/4***   
    Thank you so much, I really feel it's important to tell it as it happens, warts and all. It certainly almost never goes according to plan but I'm not one to hide the fuckups and failures as it makes for a pretty dull thread otherwise.
    Thankfully @twosmoke300has been absolutely phenomenal with his advice and obscure knowledge, otherwise I'd still be curled up in a corner of the room sobbing 😅
     
  24. Like
    fatharris got a reaction from Surface Rust in FatHarris - tales of a motoring moron ***Non-BX related content 17/4***   
    Been a lot of hits and misses this weekend.
    First up, trying to torque the camshaft cap studs was a pain, 15nm was simply not happening, even with the two nuts tight against each other, it was still turning down the shaft when close to 15nm. Tried adding a third nut to see if that would help matters, but ended up stripping the threads on the nut.
    In the end, I went for 10nm. It'll be fine, I hope. Fitted the cam, and new front cam seal before I torqued down the caps (minus one nut).

    Then it came to the camshaft pulley. Following the torque figure, I didn't even get close to the Haynes figure before disaster struck.


    That was....not ideal. I messaged Phill on a blind panic asking for advice, and he suggested drilling a 3mm hole in the bolt shank and hammering a torx socket into the hole to extract it. There were almost tears of joy when this came out.

    Then joy turned into anger when I decided to check the figures in my Autodata technical data book.
    Haynes (stated 80nm) for the sprocket bolt.

    Autodata?

    So the bolt failure was caused by a massive overtorque. Arse biscuits.
    To try and take my mind off it, I tackled some of the minor jobs, first job was removing and re-sealing the body seams around the bootlid hinge. Forgot to get any photos, but I scraped the old, dry seam sealer with a plastic scraper, masked the area off with tape and applied a healthy layer or Pureaflex40 to the joins.
    Whilst I was in the area, I managed to push the split section of the wiring rubber grommet into the hole, so it'll be a much better seal than the empty space that was there before!
    I continued the minor jobs, treating screen rust spots before they become sinister,

    Swapping out the rocker cover gasket:

    And getting this dirty bottle cleaned up as much as possible.

    Which cleaned up alright, but had highlighted how big the crack in the side of the tank was:

    As it was the rarely-used rear washer tank, I elected to try and repair it rather than replace. I used an old soldering iron to re-melt the plastic along the crack. It's not pretty, but it's sealed up and shouldn't leak so that's a win.

    The bottoms of these bottles have a sharp lip around their manufacturing joins which has been suggested aids corrosion by chafing through the paint - these were sanded down prior to install. The scuttle area had already been heavily lanoguarded about six weeks ago so all should be well there.
    Unrelated to the BX, but a mate  followed me on the commute to work and told me one of the Rovers brake lights wasn't coming on every time. Luckily, I have spare bulbs, but it was quite interesting to see the where the filament had broken loose, flapped around a bit until it made the circuit and 'tacked' itself back on. Herman has had a front fog light doing that for years, so the build-up there must be spectacular.

    Eventually, I decided to carry on with assembling the 3 pistons and liners, I'm still awaiting parts to assemble the final cylinder but this is a good start.
    Turns out I needed to order another set of piston rings too, thanks to my ill-fated attempt to fit them last time:

    Annoyingly, this was a pain in the arse. Autodoc did them at a reasonable price, but the delivery time takes the piss at around a fortnight. I found some on eBay with a two day delivery, so I placed the order on Sunday. I then sent the seller my details, and they cancelled the order! Apparently they weren't compatible. I've told them I want the rings and will assume the risk - the manufacturers of the piston rings list the set as compatible for every 1.6 XU engine except the XU52C. I can't see what difference there would be though, so I guess we'll find out in a couple of days.
    Anyway, the ring gaps were checked prior to fitment, they were all bang on at around 0.50mm.


    With the new set of plier-style piston ring compressors, I was STILL having issues with the rings. 
    I asked Phill for advice, and he very gently pointed out I was being a bit of a fuckwit and assembling the oil control ring at the bottom incorrectly, which in turn meant the ring wasn't compressing properly. 
    With the correct advice dispensed, and a slight tweak to the piston ring compressor, we were finally making progress! A fresh seal was fitted to the base of the cylinder liner before slotting it into place.

    Eventually, I got all three complete assemblies in.

    And clamped the liners down.

    Then I nipped back to the house for a pee, and noticed that Mini had snuck into MrsH's car whilst she was unloading, and got himself locked in. Tit.

    I decided to crack on with bolting in some external components, so the oil pressure switch, water pump and timing belt tensioner pulley went on (the old one was really rather grumbly and rattly)
    The pump came from Autodoc and was their own brand (RIDEX) and it seemed pretty well made.

    Next up, the crank bearing seats were cleaned, new shells were fitted, and the crank lowered into place. This was a pain in the arse with the liners and pistons fitted as the conrods were in the way, this was aided with some steel wire to hold them in the middle position.

    The crank bearing caps had fresh shells and an oiling before being loosely assembled.

    I'm still awaiting the seals for No.1 bearing cap so I've not fitted that yet.
    After that, it was applying the last coat of lacquer to the windscreen frame rust spots. The paint colour match is pretty poor, but it won't rust and that's what matters.
    I spent the remainder of the evening googling part numbers, dimensions and specs of the cam cap nut. The Citroen parts catalogue specified a nut and washer assembly, the Peugeot catalogue specified a flange nut. Seeing as this was what was fitted, I went with that, got the size and thread pitch and started searching. I eventually got three part numbers, and the phone numbers for potential dealerships that could have the nut I need in stock.
    A bit of phoning around yesterday morning ensued. The Peugeot dealership said they could source the nuts, but they wouldn't be here till Wednesday and were £1.25 each.
    My second dealership took the part number, said 'Yep, we've got 14 in stock here, and they're 63p each+VAT'. Didn't bother ringing the third.
    The dealership?

    Yep, I went in my Rover that's really a Honda, to a BMW dealership to pick up some nuts for my Citroen, which was sourced using specs from a Peugeot parts catalogue.

    The parts fella that came out was very friendly, and couldn't believe what vehicle the nuts were for I ended up having a chat with him about the Rover parked outside and he was really enthusiastic. Ended up buying 10 nuts as it makes sense to replace the entire set.
    Got home and checked the nut - it's a good fit, a bit taller and with a wider flange than the originals, it feels much more substantial. The nut is originally used to hold inlet manifolds onto various BMWs.
    I started checking valve clearances but this ended up being a pain to rotate the camshaft without the sprocket bolted in. I checked the first 4 and found them to be juuuuust within limits, I'll check the other 4 later when I've got the camshaft bolt and torqued it in.
    Boring stuff, but prepping for when it gets reassembled, the fuel pump gaskets were changed, thedistributor oil seal was replaced:

    And the inlet manifold gasket was tackled. 

    This took an absolute eternity - it was properly on there! The mating faces were eventually cleaned with a scotchbrite pad and WD40 to get a smoother mating face.

    Today, I'm into my two days off that was pencilled in for engine building - not much bloody use of I've not got all the parts together! I'll be working on various other little jobs instead.
    Cheers.


  25. Thanks
    fatharris reacted to mercedade in FatHarris - tales of a motoring moron ***Non-BX related content 17/4***   
    I won't get bored of saying it if you won't get bored of writing it up:  great work.
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